Ever since I became the new caretaker of 
Orvil's chisels, I wanted to clean them up and make new handles for them.  And having made my 
lathe recently, I could finally do it.
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| Orvil's chisels | 
These chisels had gone through some rough use.  All the handles were reinforced with steel ferrules at the back end.  The ferrules were heavily peened over from who-knows-how-many steel hammer blows.  Many of the handles were cracked or broken.
The thing I don't understand is that Orvil Heft was a carver and painter of wooden birds.  It's hard for me to imagine that he needed these heavy-use chisels.  Perhaps he collected them and didn't use them.  Or maybe he had other woodworking interests besides birds.  But whatever the case, I wanted to make them nice again to be used every day.
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| The three largest - 1 1/2", 1" and 7/8" - are Greenlee bevel edged chisels | 
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| The five smaller chisels - 3/4", 5/8", 1/2", 3/8" and 1/4" (last two not shown) - are D. R. Barton firmer chisels | 
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| The five largest chisels' handles | 
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| Right three handles are the remainder | 
To keep this post from getting too long, I'll go over the rework of the metal parts.  Next time I'll write about re-handling the chisels.
Removing the old handles was fairly easy.  Some were already loose, but some needed several raps on the benchtop to loosen them.  I took sandpaper to the metal - 180 grit and 220 grit.
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| Four cleaned, four to go | 
I was careful to go lightly over the logos.  I learned that lesson a couple years ago on a saw that I cleaned up and almost obliterated the etch.  Never again ...
When they were clean enough, I flattened the backs.  This went faster than I thought it might, thanks in part to the extra-coarse diamond stone that I got last year.  But it did take a fair amount of time, especially for the wide chisels.  Every one had low spots at the edges, possible due to being flattened on dished stones earlier in life.
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Flattening the 7/8" chisel - note the oval scratch pattern, 
showing sides and leading edge were low | 
Every one of these chisels was severely dull.  The 7/8" chisel had a big chip off one corner.  The 1/2" chisel had been rounded at the cutting edge.  And I'll get into the 1/4" chisel a little later.  All needed to be ground back to get past the rounded-over corners of the cutting edge.
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| Chip out of the 7/8" chisel | 
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| 7/8" chisel ground straight across ... | 
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| ... but this came at a price - there was a lot of material to remove to grind a new edge | 
OK, about that 1/4" chisel.  The leading edge had been ground to be 3/16" wide and the grinding started about 3/4" back from the leading edge.  I thought for a long time about what to do.  I really didn't want to remove 3/4" of usable metal and throw the length out of whack with the rest of the chisels.  My other option was to make this chisel into a 3/16" chisel.  I didn't have a 3/16" chisel, so that's what I did.
I'm not set up to do metal work.  But I went for it anyway.  Lacking layout fluid, I used a Sharpie marker to blacken the flat side and the bevel side near one edge.
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| Using Sharpie to lay out the metal to be removed | 
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| Then used a marking gauge set to about 1/32" to mark a line on the black ink | 
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Used a round chainsaw file to cut in to the gauge line as far back as I would remove metal. 
This was just shy of the D.R. Barton logo, which is on the side of the 1/4" chisel 
(the logo is on the bevel side of all other sizes) | 
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| Filed to the line | 
On the first side I did, I tried to file straight across.  But on the second side, I filed "skyward" from both directions to leave a peak in the middle.
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| Peak in middle after filing from both directions to the layout line | 
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| Then I marked the edges and filed the middle, trying not to remove the black marker all the way to the edges. | 
 After the filing, I took the sides to the diamond stones, getting progressively finer with each stone.  This gave a much better finish to the sides, but I had over-filed a few spots that will stay looking not-so-good.
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| Here's the result: from 1/4" wide to 3/16" wide (flat side shown) | 
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| Side view: logo untouched, but over-filed a bit near the start of the step-down | 
This worked out pretty well.  I got within a few thousandths of 3/16" at the business end and I'm a few more thousandths over as I go further from the cutting edge.  I can live with that.
Next time I'll write about the re-handling.